Royale Releases Test Results from New Field Discovery

Royale Energy has released the test results of the Goddard 7-1. On Oct. 15 the company announced a new field discovery near its successful Lonestar field. This week's completion activities resulted in a stabilized flow rate of 2,450 MCF per day on a restricted choke. Based on these results the well is capable of significantly higher producing rates, and the company expects to begin production at an initial rate of 2,500 MCF per day.

The first follow up to the Goddard discovery began drilling Oct 28. The Wylie #1 will test a similar nearby 3D seismic amplitude anomaly. Royale Energy will drill additional follow up wells by the end of this year.

Related Companies

Our Privacy Pledge

Most Popular Articles

From the Career Center
Jobs that may interest you
Reservoir Engineering Technician Job
Expertise: Reservoir Engineering
Location: Oklahoma City, OK
Integrity Management Engineer - Subsea
Expertise: Asset Integrity Engineer|Subsea Engineering
Location: Houston, TX
Facilities Engineer
Expertise: Budget / Cost Control|Cartography / Mapping|Facilities Engineer|HR - General|IT - SAP / ERP|Mechanic|Mining|PR / Corporate Communications|Project Engineer|Reservoir Engineering
Location: Denver, CO
search for more jobs

Brent Crude Oil : $52.72/BBL 3.31%
Light Crude Oil : $48.51/BBL 3.01%
Natural Gas : $2.89/MMBtu 1.36%
Updated in last 24 hours